Thursday, March 25th, 2010...9:52 am
Adjusted timing
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Adjusted the timing a little last night (it was reading 0tdc and I pulled it back to 10BTDC at 1000rpm idle) and added more ATF fluid to the carburetors. I had also apparently forgotten to reattach the vaccum advance and retard when I put the manifold and carburetors back on. Tweaked the timing a little after that again and it’s running like a dream with all the power it should have. I did notice that the passenger side headlight is out, so I’ll have to replace that or at the very least hit it with a multimeter to make sure it’s not an electrical problem. I suspect it’s the headlight though, I can’t even begin to imagine how old they are.
Took a photo of her this morning as I walked to work:

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